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RAYDEO

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Posts posted by RAYDEO

  1.  daleson said:

    i think raydeo should approach a journalist from stuff.co.nz or something

    Lately there have been many write up on boyracers, from stories gloryfying them to people being verbally abusive...

    would be a nice change to see a story about a bunch of people who own nice cars and do things in a decent and safe way :)

    good idea... this is the story i orginised almost 2 years ago... maybe time to do another one...

    these are all CS , southern skyline, and toyspeed dunedin members...

  2. lattest news from Bruse...

    "your crank is shagged"

    translated it means, at some stage over the last 10 years the engine has run a bearing and so engine has been replaced and the current crank has been ground down (badly) and re-used. long story short i need a new crank...

    currently looking at other options like a longer stroke

  3. to my knowledge, and someone please correct me if im wrong....

    the CEL shouldn't be on when normal driving, unless there is actually a problem, if u fix the problem the light should go out... but the code will stay in the ECU memory until cleared... so if u light is still on then I agree with kamineko, you still have an issue...

    what sensor was it? what code?

    [fixed speeling]

  4.  wildturkey said:

    have a think about taking ur pod right outta the engine bay altogether......run it under the drivers guard. Got sums pics of my leggy setup if ur interested

    watch water intake with that one...

  5.  keltik said:

    doesnt black absorb infra-red as well? Regardless - something reflective will be betterer than black

    in regards to colour... im sure it prolly wasnt the best choice... it was purely for looks... but the colour makes no difference... was just saying thats what was done on my car... its an idea...

  6. when miller made the enclosure in my GTB he just got some bendable aluminium and fut it to fit around the pod, then high enough to have about 2-4mm clearence on the bonnet, painted it black and screwed it in

  7. if the rear schocks were rooted (and lets face it it was a 1995 model car so its a high possibility) and lowered then its totally possible they wernt going too much over 100 to do that.

    Untitled-13.jpg

    the red X marks the spot where the car came to rest... from what i can figure the arrow shows what happened... the blue X is where the back wheels must have lost traction... then he basicly oversteered and hit a pole on the drivers side...

    obviously hes just a total dropkick to be doing those speeds...!!!!

  8. Just ordered parts from Liam...

    Gasket set

    cambelt

    r/c gaskets

    water pump

    water pump gasket

    oil pump

    oil pump O Ring

    clutch disc

    clutch cover

    turbo in gasket

    turbo out gasket

    to a grand total of almost $2K

    will take more pics as parts are installed...

  9. ok so the story goes...

    took her for a 800k drive through central Canturbry and Otago, got home. started up the next day and there was no oil pressure...

    turns out the oil pressure release valve was stuck open... so time for a rebuild...

    doing as much as i can in one faul swoop... and its costing a pretty penny

    New forged pistons

    race bearings

    clean and reuse rods

    clean, check, and reuse crank

    new clutch

    new cambelt

    new water pump

    new oil pump

    new oil cooler

    work started last week with the removal of the engine and pulling it apart. my suspisions were confirmed as it had a cracked piston, hence was done on compresson in one cylinder

    Raydeoengine2.jpg

    Raydeoengine1.jpg

    the block came out of the acid bath this morning.

    DSC02259.jpg

    then cleaning and boring

    DSC02255.jpg

    DSC02257.jpg

    almost ready for putting back together

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